>
> Yup watch Golby I have said it before but watch what happens.
>
> Take Care
> Arch 76 GB IL
Ok group, here is what happened. I warned you it is a long story.
In February '94 we tried to visit friends in Florida. Just inside the Fla.
line one of
those practically unheard of things happened. The head and stem of one
valve
separated and the stem ventillated the piston. We had the GMC towed off the
road to a nearby truck stop where we were able to plug into electricity
while
we decided what to do. This was on a Saturday evening. We decided to wait
till Monday morning and call Golby since at that time we had heard all good
things regarding him. Monday they came and towed us to their shop, we
rented
a car, bought a couple of coolers, loaded the car, left for home. Since the
455
motor had been a recent replacement of the 403 and (up till that point) had
been
great, we told them to just fix the problem and no more. In April they
finally
called and said it was ready. I guess they got tired of us calling them.
Since we
were both working at that time, we decided to do this over a weekend, plus
Friday. Left home Thursday night, got there late Friday afternoon. Our GMC
that was supposed to be ready to go was out on a 'road test'. When it
arrived
the first thing we noticed was glass schards on the floor just inside the
door.
They said that the door window had been shot out by vandals with a bb gun
and
they had replaced it at their expense. That didn't explain why the door was
now
so hard to close. After we got home and were cleaning it up, we found the
dent
in the top of the door which made us think that the door had been open while
the
coach was being raised on a hoist, and that was what broke the window and
bent
the door. We left Golby's Friday night and when we got back on the highway,
the
GMC felt like we had the worn out 403 back. We managed to get back home
(Newark, Ohio) sometime Sunday. This was after 2 tires blew (both on the
rear
passenger side), having to fill up with water after getting the low water
lite at
least twice, and using enough gasoline to make 3 trips. As soon as he had
time,
Gary started going thru everything. The carburetor was good BG (before
Golby).
After - the choke didn't work, the float was set wrong, and the linkage to
the
secondaries was set so that the secondaries couldn't open. Gary took the
head
they had worked on to get it pressure tested, and the water jacket had been
cut,
and they had used Chevrolet seats. After sending the head back to Golby's,
they
did replace it, but the metal gasket they sent was all bent and twisted.
They tried
to blame UPS, but the box it came in was not damaged. They had put in a
rebuilt
torque converter saying that it was standard procedure whenever they did
engine
work. Well, there was nothing wrong with the one that we had BG, but the
one they
put in put out a howl that made it very difficult to carry on a
conversation. Their
response was that some of them just do that. We sent them a list of all the
expenses
we had incurred in correcting all their screw ups, but received no response.
We
talked to their representative that was at the next GMCMI convention who
said that
they would pay for the testing of the head, but apparently he was overruled
since we
never received anything. At that point we decided that our only recourse
was to tell
everybody what we had experienced. After we started that, then we started
finding
other dissatisfied Golby victims. It sounds like Golby's business is
declining, and it
would be wonderful if we have contributed to that.
I warned you about the length of this story, but now you know.
Gary and Kara Kosier
77 EII
> Yup watch Golby I have said it before but watch what happens.
>
> Take Care
> Arch 76 GB IL
Ok group, here is what happened. I warned you it is a long story.
In February '94 we tried to visit friends in Florida. Just inside the Fla.
line one of
those practically unheard of things happened. The head and stem of one
valve
separated and the stem ventillated the piston. We had the GMC towed off the
road to a nearby truck stop where we were able to plug into electricity
while
we decided what to do. This was on a Saturday evening. We decided to wait
till Monday morning and call Golby since at that time we had heard all good
things regarding him. Monday they came and towed us to their shop, we
rented
a car, bought a couple of coolers, loaded the car, left for home. Since the
455
motor had been a recent replacement of the 403 and (up till that point) had
been
great, we told them to just fix the problem and no more. In April they
finally
called and said it was ready. I guess they got tired of us calling them.
Since we
were both working at that time, we decided to do this over a weekend, plus
Friday. Left home Thursday night, got there late Friday afternoon. Our GMC
that was supposed to be ready to go was out on a 'road test'. When it
arrived
the first thing we noticed was glass schards on the floor just inside the
door.
They said that the door window had been shot out by vandals with a bb gun
and
they had replaced it at their expense. That didn't explain why the door was
now
so hard to close. After we got home and were cleaning it up, we found the
dent
in the top of the door which made us think that the door had been open while
the
coach was being raised on a hoist, and that was what broke the window and
bent
the door. We left Golby's Friday night and when we got back on the highway,
the
GMC felt like we had the worn out 403 back. We managed to get back home
(Newark, Ohio) sometime Sunday. This was after 2 tires blew (both on the
rear
passenger side), having to fill up with water after getting the low water
lite at
least twice, and using enough gasoline to make 3 trips. As soon as he had
time,
Gary started going thru everything. The carburetor was good BG (before
Golby).
After - the choke didn't work, the float was set wrong, and the linkage to
the
secondaries was set so that the secondaries couldn't open. Gary took the
head
they had worked on to get it pressure tested, and the water jacket had been
cut,
and they had used Chevrolet seats. After sending the head back to Golby's,
they
did replace it, but the metal gasket they sent was all bent and twisted.
They tried
to blame UPS, but the box it came in was not damaged. They had put in a
rebuilt
torque converter saying that it was standard procedure whenever they did
engine
work. Well, there was nothing wrong with the one that we had BG, but the
one they
put in put out a howl that made it very difficult to carry on a
conversation. Their
response was that some of them just do that. We sent them a list of all the
expenses
we had incurred in correcting all their screw ups, but received no response.
We
talked to their representative that was at the next GMCMI convention who
said that
they would pay for the testing of the head, but apparently he was overruled
since we
never received anything. At that point we decided that our only recourse
was to tell
everybody what we had experienced. After we started that, then we started
finding
other dissatisfied Golby victims. It sounds like Golby's business is
declining, and it
would be wonderful if we have contributed to that.
I warned you about the length of this story, but now you know.
Gary and Kara Kosier
77 EII