Not sure what I have posted here on the subject. couple sundays ago, driving down the freeway things all is good, the coach started loosing some
speed and pressing on the gas a little it kept dropping down. I noticed some smoke behind, so I shut off the engine and coasted to a stop.
I found oil on the front driver side of the engine, and the final drive was coated. everything else looked OK, so I opened up the hatch and started
the engine:
https://youtu.be/h-MP_AqBboI
Luckily it was Sunday on our way home, only 8 miles to go. I sent the wife and kids away in the towd and waiting an hour for the tow truck to come
and give me a ride home.
my friend came over and it was pretty much verified that it was internal and the engine had to come out. Last Saturday, some friends came to help,
and had the engine, final drive and tranny out of the coach. The transmission made it way to the rebuilder this morning.
Anyway, today I pulled off the oil pan, and found my issue. #6 piston seems to have a good hole and beat to hell. The spark plug is busted, and
looks like the push rod is falling off the lifter. I also pulled that valve cover and noticed the prior mechanic had left the spark plug organizer
inside the valve cover.
http://www.gmcmhphotos.com/photos/member-galleries/p65126-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65125-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65124-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65123-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65122-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65121-engine-failure.html
Time to start cleaning the garage and parts. Have some work to do the next few weeks.
--
Jon Roche
75 palm beach
St. Cloud, MN
http://lqqkatjon.blogspot.com/
speed and pressing on the gas a little it kept dropping down. I noticed some smoke behind, so I shut off the engine and coasted to a stop.
I found oil on the front driver side of the engine, and the final drive was coated. everything else looked OK, so I opened up the hatch and started
the engine:
https://youtu.be/h-MP_AqBboI
Luckily it was Sunday on our way home, only 8 miles to go. I sent the wife and kids away in the towd and waiting an hour for the tow truck to come
and give me a ride home.
my friend came over and it was pretty much verified that it was internal and the engine had to come out. Last Saturday, some friends came to help,
and had the engine, final drive and tranny out of the coach. The transmission made it way to the rebuilder this morning.
Anyway, today I pulled off the oil pan, and found my issue. #6 piston seems to have a good hole and beat to hell. The spark plug is busted, and
looks like the push rod is falling off the lifter. I also pulled that valve cover and noticed the prior mechanic had left the spark plug organizer
inside the valve cover.
http://www.gmcmhphotos.com/photos/member-galleries/p65126-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65125-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65124-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65123-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65122-engine-failure.html
http://www.gmcmhphotos.com/photos/member-galleries/p65121-engine-failure.html
Time to start cleaning the garage and parts. Have some work to do the next few weeks.
--
Jon Roche
75 palm beach
St. Cloud, MN
http://lqqkatjon.blogspot.com/